Dynahoe Steering Rebuild
Removing the Kingpin turned out to be a project. A 10Lb hammer had no effect.




This rig is a 10' length of 1-1/2" EMT conduit. Strapped to the EMT is a length of Unistrut. At the top is a pully. Inside the EMT is a 20Lb piece of 1-1/4" bar stock. I welded a loop to the top end of the bar stock, and tied a rope to it.




The rope goes up and over the pully.




Close up of the pin. There is a washer sitting on the king pin to prevent mushrooming the king pin. This allowed me to repeatedly drop the 20Lb "hammer" from over 8 feet. Even repeated impacts from this didn't move the pin until I heated the middle part of the crossmember to 260+ degrees.




The washer before and after.




The crack in the block was not there before using the rig! That is an 8 x 16 x 4 solid concrete block.




The holes were also worn out of round. The shaft and bearings are old theater dimmer parts. I drilled a hole for a small cobalt lathe bit held in place by a set screw. Careful shimming involved to get the shaft close to the original centers. Used my 1/2 drill to turn the shaft. Light cuts worked best. The collar was used as a stop for the bottom bore, which I left at the original ID below the snap ring groove.




Bushing with groove and holes (3) for grease flow.




one of 3 grooves to bring the grease to where the highest load is.




The bushings installed in the knuckle. They are a light press fit, with set screws were added to help keep the bushings in place.




Test fit of the kingpin.




All re-assembled.


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