Santa Fe FM Trainmasters
Part 3
Copyright 2004 J.
Sing, V. Niner, R.
Gustafson - All Rights Reserved
The Flagstaff
Incident: Countdown
Unfortunately, teething
problems began
occurring during the Stage 3 testing. These issues
resulted in the most serious
breach of the tight security for the whole project, the
'Flagstaff Incident', which
occurred
on April 1,
1955.
Santa Fe 3150 was on a Stage 3 test run number 13, eastbound,
racing over the crest of the Arizona Divide aiming yet again for the
Winslow home base 'black ops' enginehouse
before
dawn. With US Department of Commerce military infrared imaging,
we are able to see what
occurred.

Santa Fe 3150 was hitting 80 MPH, racing like the wind eastbound,
uphill past Kendrick towards the Arizona Divide at Riordan.
As the Super Trainmaster roars past the signal bridge at Coconino,
an alarm bell goes off...... and smoke appears coming out
of the insulation and brushes of the
#2 traction motor.
The Flagstaff Incident:
President Gurley
Unbeknownst to all concerned, at that very
moment, Santa Fe President Gurley and his inspection train had
arrived
at West Riordan on an unannounced inspection
tour of the
Third District of the Albuquerque Division. At that early morning hour,
Mr. Gurley was waiting on the balcony of his
presidential car to
see a glimpse of his prized Black Ops 'Project 3150':
As the Super Bee test train came into view, to Mr. Gurley's chagrin,
the Super Trainmaster was slowing rather than racing......
The insulation fire on the #2 traction motor
had caused a flashover on the main generator, and the Trainmaster
was
behaving much more like an Alco at that moment,
right in front of ATSF President Fred Gurley's eyes:
It was not the best of times for Fairbanks Morse.
Reconnaissance at Riordan
Special Assistant V.G. (Norm) Viner had no choice except to move
the smoking Super Trainmaster onto the RIP track in the West
Riordan enginehouse for an emergency
inspection.
FM Black Ops engineer J.M. Singer examined the smoking #2 traction
motor. The aghast graveyard shift mechanics look
on, dumbfounded, at the sight of an engine they know for
sure doesn't exist.
The West Riordan roundhouse team, of course, were unable to effect
repairs on a
'black project' engine. The decision was made to cut
out of operation the #2 traction motor, reset
the main generator, and continue on the remaining five traction
motors over the Arizona Divide on through Flagstaff and back to Winslow.
With smoke still wisping in the air, and sunrise now upon them, the
Super Trainmaster left Riordan, hoping to make it home to Winslow with
a bare minimum of exposure.... but
daylight is not kind. A very late Grand Canyon streamliner whistles
by....... with the passenger F's engine crew gawking at
the sight of the mystery engine.
So now, the race to evade detection was on.
Onward to Flagstaff!
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