LX10 Fixes


Contrary to conventional belief, the LX10 has a pretty good drive system and mount that is more than good enough for astrophotography (consider the fact that for decades photographs were taken with early Meade and Celestron SCTs that had drives significantly inferior to the LX10's).  There are a few simple improvements that can be made, however, that can improve the scope considerably.

Note:  I recently was lucky enough to be one of two main developers of a new small local public observatory.  (See http://indianastars.us).  One of the scopes we have there is a 12" LX200, so now I've had a good chance to compare the LX10 with the LX200.  Mechanically, I haven't noticed a significant difference in stability, accuracy, etc.  Mostly the LX200 has some computerized features (mainly periodic error correction and backlash compensation) and quartz regulated drive rates that improve the accuracy of the drive system.  But the LX10 is still more than good enough for photography.  I took passable pictures with my first "serious" scope, an original classic Celestron C8, over 20 years ago.  By comparison, the LX10 has hundreds of dollars worth of improvements over that scope (e.g., worm drive vs. spur gear, built in RA drive corrector, etc.) for essentially the same price I paid 20 years ago (price not corrected for inflation!).

See also my page on how to connect an autoguider to an LX10, with samples of my LX10 astrophotography.
Questions or comments?  Email me at jmmahony@hotmail.com.

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Tripod

The tripod normally sold with the LX10 is uncomfortably short if you want to use it from a standing position (it  looks a bit weak too, but I haven't had that much experience with it).  Fortunately the tripod is sold separately so you can just get the standard adjustable tripod (normally used with the LX200) instead for a little extra money.  For a cheaper and lighter solution, see if you can find one of the old "locked triangle" tripods that were made for the original classic Celestron C8.  These were remarkably rigid and very light.  The only drawback is that for storage, the legs fold up (over the head) rather than down, which makes them a bit awkward to set up until you get used to it.  Fortunately, the light weight makes that considerably easier than it sounds.  The central hole in the head is only 1/4" rather than 1/2", so you'll need a 1/4" bolt and a bushing (spacer) for the hole in the Meade wedge.
 

Wedge

This works pretty well.  I replaced the tilt plate clamping/coarse adjustment bolts with hand-knobs (see http://www.scopestuff.com) since the tilt has to be adjusted slightly each time it is set up, unless you regularly set up on a level paved surface (which should be avoided-heat from a paved surface will cause image-degrading turbulance in the air, and vibration-dampening is better on a dirt surface).  I couldn't find a hand-knob with a long enough shaft to replace the adjusting screw, so I just used a length of 1/4" threaded rod with the end bent over to make a handle, which has worked very well.
 

RA Drive

The LX10 has a good worm drive with about 1 arcminute periodic error (similar to the LX200, before applying the LX200's periodic error correction).  My only complaint is that it uses a simple DC motor with a voltage-regulated power source.  Quartz regulated systems are cheap today so that would have been better. The system is stable enough for the time period required for a single exposures, but from night to night, as temperature variations and battery power affect the drive rate, you'll want to know about the variable resistor (accessible through a panel on the bottom of the drive base) that can be tweaked to affect the drive rate.  Since this control is hard to get to, you may want to remount it somewhere on the front of the scope.  See also this part of my Autoguided LX10 page for info on replacing this 500 ohm variable resistor with a 200 ohm variable and 300 ohm fixed resistors for better control.
 

Declination

In a recent review of several small telescopes, Sky&Telescope commented on how frequently simple, easily avoidable design errors show up in telescopes.  Meade has a reputation for good optics, and their computer systems generally seem better thought out than Celestron's, but their weak point is mechanical design.  On the LX10, this shows up in the small threaded part at the end of the tangent arm (see picture).  The arm itself seems to be made out of a special, extra-stiff, aluminum alloy, but after going through that extra trouble, the simple threaded part that the dec fine-adjustment screw goes through has multiple problems.  First, it could have been made almost twice its diameter (for less play between it and the arm) without limiting the range of motion of the arm.  But even worse, it is only threaded for about half of its diameter (the rest is bored out to a larger, non-threaded size).  This leaves only about 1/4" of threaded hole, which means the fit between it and the dec adjustment screw is sloppy, causing some backlash.  If you have access to a metal lathe, I would suggest making your own replacement part, but if not, a simple fix is to drill and thread a small hole perpendicular to the dec adjustment screw-hole in this part and put a small nylon thumb screw in it, so that this screw presses sideways against the dec adjustment screw.  That presses the dec screw against the threads to remove the play.  Using a thumbscrew allows this to be loosened for visual use, so that the dec screw turns easier for easier manual dec adjustment.

Note the narrow inch long black screw parallel to the dec adjustment screw and above it, on the tangent arm.  This screw was loose in the box when I got my scope, and I only recently (after seeing someone else's LX10) found out what it's for. As you can see in the picture, the tangent arm is split at the end and the screw can be tightened for a better fit between the split end of the tangent arm and the small part that forms the connection between the dec adjustment screw and the tangent arm.  I haven't experimented with this yet.
 

Dec Motor

For deep-sky photography, you'll need the dec motor (sold separately).  Mine works well, with insignificant backlash.  The only part I had a problem with was the clutch.  The motor tucks under the fork arm, and has a small gear on the shaft.  You take off the rear dec fine-adjust knob and replace it with a plastic hub that has a larger gear on it that meshes with the motor gear.  Like most such dec motor assemblies, there is an adjustable clutch that allows you to use the dec knob either manually, or via the motor, or both.  The clutch can be adjusted tight, for motorized control during photographic guiding, or loose, for manual control during visual use, or partially tightened for both.  The problem in this case is the way the clutch adjustment works.  The large gear goes over the hub on the end of the dec screw, with a slightly loose fit. There is a plastic cap over the end of the hub that presses the gear against a rim on the hub, for clutch action.  The cap has a small hole in it that fits over a tiny 1/2" long #4-40 threaded stud that is threaded and glued into the end of the hub.  A nylon-insert type locknut is threaded onto the end of the stud.  If you tighten the nut, it presses the cap against the gear, which gets squeezed between the cap and the rim on the hub to increase the friction.  There are two problems with this:  first, if you have it adjusted partly tight for both manual and motorized use and turn the front dec knob, the clutch-cap tends to rotate against the locknut and tries to turn it.  This is why Meade uses a locknut, but the torque on the stud can end up breaking the glue loose and loosening the stud.  Second, the dec knob is a rather "fine" control, so it has to be turned a lot at medium or low power to make a difference.  The dec screw has a lot of friction when the clutch is "partly" tight, so using this setting will wear your fingers out quickly.  Thus you'll be adjusting the clutch a lot to go from loose (fully manual) to tight (motor control).  If you use a small wrench on the nut, you'll risk breaking the glue on the stud, so the end of the stud has a small hex hole in it that you're supposed to put a tiny allen (hex) wrench in to keep the stud from rotating.  But with small parts, and with very little slop in the motor, it's difficult to keep the tiny hex wrench in a fixed enough position.  Further, using these small tools is a pain in general, especially when you're working in the dark.  I eventually broke the glue (I think I forgot to use the hex wrench at least once).  Rather than trying to reglue it, I used a small 4-40 screw that I threaded through a nylon wing nut first (with the "wings" toward the head end of the bolt) and left out the locknut.  The wingnut takes the place of the locknut, and is very easily switched from tight to loose.  When it's in the fully tightened position for motorized guiding, it's tight enough to not come loose (no glue or locknut needed).  It's very easy to loosen for manual use, and I haven't had any trouble with the 4-40 screw loosening.
In my case the stud had already come loose, so I figured using a normal screw with a head would prevent the wingnut from ever fully unscrewing and falling off and getting lost, but I've since heard from others who left the original headless stud in and just put the wingnut on that (minus the original locknut, of course).  They haven't had any problem with the wingnut coming off.
 

Finderscope

In a letter to the editor of Sky& Telescope, (in reference to the above mentioned article) a reader pointed out a manufacturing error in the 6X30 finderscope that Meade (and Celestron) uses.  I discovered this error by accident:  the field lens of the finder's eyepiece is installed backwards.  The manufacturer (some generic scope accessory maker, not Meade itself) has apparently been doing this for years.  The finder has a focusing adjustment, but the reversed lens affects the adjustment range and may also (depending on your eyesight) make the crosshairs out of focus.  Fixing this is easy:  unscrew the eyepiece end and take out the plastic press-fitted retaining ring.  Be careful!-the rest of the parts slide out of the eyepiece tube easily then!  Make sure you keep everything in the proper order and orientation.  Also be careful of the crosshairs: they're made of extremely thin wires and can be easily damaged.  I don't recall the exact order of the parts, but the eyepiece has two lenses, and the field lens is the one further from the eye (so it will be the first one you get to as you take out parts).  Simply reverse the field lens and then reassemble everything.
 

Battery Pack

I suspect Meade realized too late that the 9V battery doesn't last too long.  They seem to have put in the AA(X4) battery pack as an afterthought, and you have to remove the bottom panel to get to it, which is a pain (no, it doesn't fit into the 9V battery compartment, at least not on mine).  There's an easy fix for that:  if you read my Autoguided LX10 page, you know that the external power jack can actually use any voltage level down to 6V (it's wired identically to both the 9V and AA battery sources-the first stage of the voltage regulator reduces any of these to a common lower level that the rest of the drive circuitry uses), so all you need to do is remove the plug on the battery pack and put on a plug that fits the external power jack (5.5 mm O.D., 2.5 mm I.D., readily available at Radio Shack.  The center pin is positive.)  Now you can just plug the batteries in to the external jack, and leave the batteries sitting on the base plate of the wedge, or maybe find some way to attach the battery holder in a covenient place on the drive base.

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