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Click on the pictures for a larger view:
A helix is inside this as of yet
treeless mountain. The original track work began to cause problems so I decided
to re-do it. Following you will see how I improved the helix. |
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The helix is
built with what I call "stadium seating". The spiral radius increases as it
rises. That way I can reach rolling stock easier. The original configuration had
a diameter of 29 inches at its smallest (lower most level) increasing to 39
inches at its maximum (top level). There were 3 1/2 turns total. The track was
Peco flex laid loose with the rail joints soldered. The plan was that the loose
track would allow for expansion and contraction. In reality I found the rail
joints began to form a set with a somewhat slight kink. I believe this was due
to the expansion of the track and the soldered joints were deforming. As time
went on trains began to perform less reliably. The rise, diameter, and
deteriorating track work combined to restrict train lengths running through the
helix. A solution had to be found! |
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Here is a closer
view of the original track. The spiral was cut from Homosote with
stepped riser supports. I made the spirals wide enough to center the
track . I studied this setup for quite awhile testing my assortment
of engines and rolling stock. I felt two factors contributed to the
problem. First the rise was an issue. I needed to find a way to
reduce the grade. The second was the kinks forming at the rail
joints. |
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By narrowing the width of the spiral turns (1 1/4 inches) I was able
to increase the total turns to 4 1/2 from 3 1/2. This lowered the rise
improving the grade. The minimum and maximum radius did not change.
I placed the track right at the inside edge of the spiral this time.
Because the radius increases I only had to concern myself with
clearances on the outside of the curves. With the improvement of the
grade I concentrated on eliminating the kinks in the track. Peco
track does not want to maintain the curve. Without some way to hold
it in place it wants to straighten out. Micro Engineering track on
the other hand will stay curved on its own. By switching to ME track
less tension would be transferred to the rail joints. This allowed
me to not solder the rail joiners. I did run track feeds to each
section of flex track to insure conductivity. |
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This closeup will show the ME flex track glued to the Homosote.
Notice how the inside edge of the ties are even with the inside edge
of the spiral. You can also see the stepped support and how the
spiral radius increases with each level. Gluing the track
permanently keeps the curve properly placed on the roadbed. |
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The rail joints
were left unsoldered and gaps in the rail allows for expansion. This
system has been operating for about one month and so far has
performed faithfully. Eventually the mountain will be covered with
trees and access will be only by the hole in the benchwork inside
the helix.
I believe my
efforts have been rewarded in better operation and recommend this
technique to others. |